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Chronology of the ATF3 by John Evans

Revised March 5, 2002

PRELIMINARY (Living Document)

NOTE: Information in this Chronology was compiled from memory by John C. Evans. The "dates" and some of the "facts" are not totally accurate. If you have information or corrections please contact me at jcevans@fastq.com.

To the best of my memory this is a chronology of the ATF3 program. All information prior to my hire-in on December 2, 1968 should be considered hearsay and may be very inaccurate.

For a description of the original ATF3 engine configuration see link: Aviation Week Article

Around 1966

1967

1968-1969


1971-1975


1975


1975-1980

May 15, 1981

February 1982

1983 to Present

ATF3 Production Engine Performance Ratings and Aircraft Applications

Engine Model

Thrust Rating Cold Day

Thrust Rating   Hot Day

Aircraft Application

ATF3-All

6000 Maximum

1850 Deg F ITT  (1010 Deg C)

Maximum Certified Thrust and ITT for all ATF3 Engine Models

F104-GA100

4050 to 86 Deg F

Teledyne-Ryan Compass-Cope    YQM-98A

ATF3-6-2C

5440 @ 59 Deg F

5050 @ 76 Deg F

U. S. Coast Guard HU25-A (F20G)

ATF3-6-4C

5440 @ 59 Deg F

4747 @ 86 Deg F

U. S. Coast Guard HU25-A (F20G)

ATF3-6A-3C

5440 @ 59 Deg F

5050 @ 86 Deg F

French Navy Gardian (F20H)

ATF3-6A-4C

5200 to 80 Deg F

5050 @ 86 Deg F

Falcon 200 (F20H)

IN-SERVICE MAJOR ENGINE DESIGN UPGRADES

· Engine Main-shaft Carbon Face-Seal Cartridge Fix. The #1, #2, #3, and #4 bearings used cartridge type carbon face seals that had a propensity to stick and leak. The floating carbon seal was redesigned to a two piece seal using a Carpenter 42 steel ring, holding a carbon face seal with a narrowed and repositioned sealing surface. The secondary "O" ring seal material was changes to reduce oil-induced swelling and sticking.

· High Pressure Compressor Surge Fix. The high-pressure compressor shroud profile was changed to more closely match the compressor rotor blade profile at high power. A series of holes were also added to the shroud near the rotor blade inlet to match rotor blade inducer (inlet) flow to the blade exit flow throughout the engine operating range. The high-pressure rotor tip clearance was reduced with the addition of the "Huber Bump" to the HP Diffuser. These design changes were created and tested by Engineer John T. Huber at Site B.

· Low Pressure Compressor Surge Fix. The low-pressure compressor was redesigned to improve surge (compressor stall) margin. The fix included 0.020" shorter 2nd stage compressor blades, a 2nd stage blade tip shroud with three stiffening rings, staggered stator anti-rotation lugs, redesigned 5th stage blade tip and shroud angles, and an interrupted 5th stage stator. This fix eliminated 2nd stage compressor blade failures and low-pressure compressor surges. Engineer Mike James was instrumental in the flight test program defining the surge problem as a severe 2nd stage low pressure compressor high altitude blade tip rub that negatively impacted blade tip efficiency.

· #4 and #5 bearing Carbon Seal Fix. The carbon seals were redesigned from a ring type seal to a segmented ring seal, and the metallic cartridge was redesigned to prevent coning of the sealing face. The seal rotor sealing face was coated with Tungsten Carbide for durability.

· #1 Main Bearing Carbon Face Seal Fix. The seal overheated and failing in operation. An oil jet was added to cool the #1 carbon seal rotor resolving the problem.

· Inlet Guide Vane (IGV) Cable Fix. As certified ATF3 engines had an aft mounted IGV Actuator (on the accessory gearbox) controlling the inlet guide vane positioning in the engine inlet. A "Hard-Linkage" I-Bean type linkage with bell-cranks and bearings attached the Actuator the Vane "Unison-Ring" controlling the vane position. This design was a maintenance nightmare requiring removal on the nacelle tail-cone and lubrication of the bearings every 25 hours of engine operation. A" Teleforce" cable system had been designed and tested by Engineer John T. Huber at Site B during ATF3 certification appeared to be the solution. John C. Evans was able to introduce the Teleforce cable into the fleet as a Field-Evaluation program, which was immediately embraced by the aircraft Owners-Operators and Maintenance personnel. The cable system extended the IGV inspection interval from a 25-hour lubrication to a 250-hour torque check.

· Electronic Engine Control (EEC) noise reduction fix. The EEC was redesigned to reduce engine inlet noise by more than 30 dbA at idle. The fix repositioned the inlet guide vanes from 40 degrees to 0 degrees below flight idle. The repositioning only occurred on the ground when engine powers below flight idle were selected. Two additional fixes were incorporated. The low-pressure compressor surge fix allowed a change to the inlet guide vane schedule. This change prevented a surge protection schedule from closing the guide vanes at high altitude cruise improving engine high altitude performance and durability. Adding a solenoid to the Generator Control Unit (GCU) circuit improved durability.

· Oil Consumption and Leakage Fix. The ATF3 engines had an oil consumption problem when operating above 24,000 feet. Oil consumption would increase to as much as one quart every 25 hours. The problem was traced to accessory gearbox seals. The Viton shaft lip seals were replaced with Graphite filled Teflon seals and the permanent magnetic generator (PMG) carbon face seal was redesigned virtually eliminating the oil consumption problem.

· "Silver Bullet" Fix. The silver bullet is the traditional method of killing Vampires (in our case low engine overhaul intervals and high maintenance costs). The concept was based on the results of revised fan turbine cooling testing designed and conducted by John T. Huber at Site B. Primary players in the "Silver Bullet" redesign were Engineering Manager A. W. (Fred) Fuller and a recently hired Engineer Kurt Lammon. The primary focus of the silver bullet modifications was to reduce and better control turbine section metal temperatures to extend operating life and reduce repair costs. This was accomplished by revising cooling flows and controlling them with additional metal baffles, revised piston ring seals, and extensive use of ceramics. The design changes also prevented combustion products from entering the engine cooling air passages and contaminating aircraft cabin air. Emphasis was placed on reworking and reusing existing hardware to keep conversion (and engine operating) cost to a minimum. This program was a huge success, reducing turbine metal temperatures by as much as 350 Degrees Fahrenheit and extending fan turbine disk cycle lift threefold.

· 4th Turbine "Paired-Seal" Labyrinth Seal Fix. As designed the ATF3 engine had a 12-inch diameter 4-step knife-seal on the forward side of the 4th turbine disk. This seal had a 0.018-inch radial clearance and was sealing 80-psid air. The seal spacing was only 0.220-inch, which was not adequate for the relative thermal movement of the knife seal to seal land. A "Paired-Seal" four-knife seal was conceived by John C. Evans. The seal consisted of two pairs of two knives, each pair riding on one of two diameters of the seal-shroud. This change increased seal land width from 0.220-inch to 0.450-inch, doubling the allowable seal axial travel. Seal radial clearance was reduced from 0.018-inch to 0.008-inch reducing loss of turbine cooling air and resulting in 16-Degrees Fahrenheit increase in engine temperature margin. The "Paired-Seal" fix was incorporated into in-service engines at the same time as the "Silver Bullet" Fix.


Revised 3/21/2002